Freeport LNG provides summary of root cause failure analysis report on June 8 incident
Freeport LNG is today providing the results of an independent, third-party root cause failure analysis (RCFA) report on the June 8, 2022 incident that occurred at its liquefaction facility.
The RCFA report was commissioned by Freeport LNG and independently conducted by a highly qualified incident investigation company, IFO Group, in order to identify the causes underlying the June 8th incident. Over the course of almost five months, IFO Group investigated the incident, collected and analyzed physical specimens from the incident, interviewed witnesses, reviewed process and design data, and ultimately developed the RCFA report, identifying specific causes that led or contributed to the June 8th incident. The safety and security of our workforce and surrounding community, and environmental stewardship are Freeport LNG’s top priorities. Freeport LNG believes that transparency around the causes of this incident, and the remedial actions it is taking to ensure an incident of this nature never occurs again, is critical to maintaining public trust. With that in mind, the results of the root cause failure analysis prepared by IFO Group are as follows:
• Isolation of a piping segment containing cryogenic liquefied natural gas (LNG) without proper overpressure protection, which LNG then warmed and expanded due to exposure to ambient conditions, resulting in a boiling liquid, expanding vapor explosion, or BLEVE, and the rupturing of the piping segment.
• Pressure safety valve (PSV) testing procedure and car seal program deficiencies; • Failure to repurpose temperature indicator alarms used for cool down operations during commissioning on LNG piping that could warn operators of increasing temperatures in LNG piping during operations; and
• Operating procedures that allowed operator discretion to close valves that could allow LNG to be isolated in a piping segment.
• Failure of 2016 Hazard and Operability study to evaluate the potential for a blocked-in LNG piping segment with inadequate overpressure protection;
• Failure to utilize management of change process for revisions to tank management operating procedures;
• Failure to accurately and timely diagnose sudden pipe movement as being due to piping stresses from the overpressuring of an adjacent piping segment; and
• Operator fatigue as a result of significant overtime needs. IFO Group proposed recommendations to resolve each of the above root and contributing causes, and Freeport LNG is implementing each of those recommendations.
Specifically, Freeport LNG has made significant enhancements to its PSV testing processes and car seal program, implemented procedural changes to avoid operating scenarios that could allow blocked-in LNG in piping segments, and revised its control system logic to alert control room operators to valve positions or temperature readings that indicate possible isolation of LNG in any piping segments. Freeport LNG is also updating its training program to address causes of the incident, as well as identification and diagnosis of abnormal operating conditions in the facility.
To supplement IFO’s report, Freeport LNG also engaged another independent consultant to perform a full review of its LNG storage and transfer operating procedures, its control systems maintenance and inspection procedures, and its personnel qualifications and training programs.
As a result of this independent, multi-month review, Freeport LNG is implementing various recommended improvements in these areas. Additionally, Freeport LNG has undertaken a significant hiring effort to increase LNG plant employee staffing by over 30%, in order to reduce the amount of overtime, as well as create new functional departments within the organization that are focused on improved training, operational excellence, quality assurance, and improved business performance.
Freeport LNG is also executing an extensive company-wide process safety management initiative to apply and reinforce process safety concepts into daily work processes across the organization. Freeport LNG is committed to emerging from the June 8th incident with an unmatched focus on safety, operational integrity and operational excellence.
Modern society would not be possible without the use of pipelines to transport natural gas, crude oil and finished products to demand centers.
Optimizing Gas Distribution: Accounting for Changeovers, Regulators, and More
Gas distribution systems are critical to the effective operation of many industrial facilities around the world. Despite the importance of these systems, however, opportunities to improve their performance and cost-effectiveness are often missed or misunderstood. Increasing changeover pressure may seem like a good way to improve system flow, for example, but it often does so at the expense of bottled gas. Adding regulators may help you control supply pressure, but it also adds cost to your system. So, how do you know what the ideal gas distribution setup is for you?
Attend this webinar to:
- Gain a basic understanding of the fluid dynamics that affect pressure control in gas distribution systems, learning to interpret flow curves and recognize phenomena like lockup, droop, and supply pressure effect (SPE)
- Learn how inlet pressure affects regulator performance and when to specify certain regulator types and configurations to effectively control gas system pressures
Understand the inherent trade-offs between gas utilization and flow capacity and how to select both the right changeover pressure and automatic changeover panel design for your operations.
May 4, 2021 10:00 AM CDT